Polishing
The polishing tool was made from four disks of 20inch diameter exterior
plywood and one piece of 18 inch diameter 45mm thick worktop glued and screwed
together. A strip of wood 2x1was also added in the middle of the top piece
and overhanging the edges a few inches helped lifting the tool off the mirror
face. The edges where sealed with PVA glue and painted all over with white
exterior paint. The edges where then sealed again, after the pitch lap was
complete, with fibreglass resin to seal again and also prevent flaking of
paint. The tool has to be thick to prevent flexture and inducing astigmatism
into the mirror during polishing.
2 1lbs of cerium oxide and 3 1lbs of optical pitch were purchased for the
polishing process. Geoff and I made the pitch lap on the 6/6/97. The pitch
was broken up into small pieces before adding it to the pan. It was during
this that Geoff noticed something shiny in the pitch. On inspection it was
found to be aluminium swarf. More pieces where found and we had to scan all
pieces before they where added to the pan. The pitch was heated in an old
pan using a petrol gas camping stove on a low heat so as not to boil the
pitch. The lap was pre-formed with car body filler the same as the previous
tool and wiped with turps to give a clean surface (sheen, but not wet). The
lap was duct tapped to 1/2 an inch and the pitch (now a runny honey consistency)
was poured in a spiral from the outer edge to the middle. A dollop was made
in the middle to form a higher area, When the pitch began to set the dam
was removed. This proved a problem as the dam had stuck to the pitch and
began to damage the pitch lap. We waited another minute for it to go harder
and used a Stanley knife dipped in water to cut the dam away. This waiting
proved to be a problem as the lap had set too hard and when we pressed the
lap into the mirror, after wetting and soaping (washing up liquid) both surfaces
well, the lap did not fully take up the shape of the mirror. The outer facets
where touching but the middle was not. We heated the lap 6 or 7 times with
a portable heater and blowlamp and repressed each time. Eventually most of
the facets where touching. This was not easy work and took some time to complete.
During each press we cut the facets out with a saw so that to pitch had somewhere
to goto. Some damaged or stubborn facets where repaired by adding a small
amount of pitch off a spoon or by putting a small amount of pitch dust on
the surface and flashing the blow lamp across to melt it in.
![[Image]](pict19.jpg)
Above shows Geoff Regan pouring the melted pitch onto the pre-formed
tool.
![[Image]](pict20.jpg)
Above image shows the completed lap ready for use.
We cleaned up all surfaces, hoovered and changed
the plastic sheets. The floor was dampened and all doors shut. Cerium oxide
was added to a clean sauce bottle. 6-heaped teaspoons to a full bottle of
water. A spiral was added to the mirror and tool. The surfaces where misted
with the spray bottle and we began polishing. We began with normal back and
forth strokes with a 2 inch overhang, each stroke lasting 4-5 seconds. The
tool was sticking in places and difficult to move at some points. The tool
quickly came to equilibrium and was easier to move. Slight W strokes where
then used of 3-4 seconds having a slow consistent drag (this is when most
effective polishing is done). We did 30-40 minute sessions at a time
and checked the tool each time. The facets at the outer edges became tinted
with the colour of the cerium oxide and began to touch more and more towards
the middle as polishing went on. Polish on the mirror was seen after only
40 minutes work and in was noted that it was more polished in the middle
zone than at the edge or middle (annulus shaped). This gradually widened
and became more polished and the middle began to have more polish also. After
2 hours 40 minutes we stopped work and decided to do a focult test. The mirror
was removed and mounted in the test rig. The mirror appeared to show slight
astigmatism with a central depression. This later proved not enough polish
was done on the edge to test for a turned edge.
On the 14/06/97 we began work by cleaning the work area, washing the mirror
and the damming the tool and pouring on hot water ready to press. After scolding
Geoffs hands we removed the dam after only 30 seconds, soaped the mirror
surface and pressed the mirror down until cool. The tool had been covered
over the week with cling film. This had imprinted shapes and wrinkles into
the pitch and did not get fully removed by the cold press. We began work
with normal strokes for 1/2 hour and then went onto W strokes for the rest
of the session. We completed work after 2 hours and 20 minuets. By now the
mirror showed much more polish with only the outer edge and a small central
region requiring more work. The tool was well covered in cerium oxide and
water then covered with thicker plastic sheet instead of cling film. The
mirror was placed in the test rig and a focult test done at 1800 hours. This
showed uneven shadows at the centre but the same if not slightly improved
knife-edge inside of focus. The mirror was retested at 2300 hours and showed
a much clearer figure. This was attributed to the mirror cooling down evidence
of this cooling was noticed by Geoff during the earlier test at 1800 when
the shadows appeared to be changing slightly.
What was most striking was that it had appeared that we had mis-interpreted
the results of the test the previous week. This time it was very obvious
at 2300 hours that the mirror had a raised ring near the edge and a large
raised hill running from the base of this ring to the centre of the mirror
and not a depression. But see below!!
Caution !! When checking other readings on mirror figuring one showed focultgrams
through the stages of sphere to hyperaboliod. The oblate spheroid looked
remarkably similar to the foucult test done on the 14th. Shadows change side
from left to right going from oblate spheroid to paraboloid.
One interesting test was placing a thumb on the mirror while doing the focult
test. Big hill, very bright on the right and dark on the left. Thermals off
hand very prominent.
Another was placing a bag of peas in the centre too cool the middle. This
had the effect of deepening the centre after only a few seconds!!
One solution to storing the lap between polishing sessions was to let the
lap dry out and then cover with one sheet of newspaper. This did not stick
to the surface or make any imprints on it. This has now been done many times
successfully.
Figuring the
mirror
1) Making an 8" tool to bring down the centre
The centre of the mirror was way too high and we decided to lower it to a
better shape before we did any more polishing. This would be done with a
sub diameter lap of 8". On the 6/9/97 we made the 8" lap. Lessons learnt
by Geoff when doing the 6 inch finder scope mirror where not to form a dam
at the edge of the tool as this will build up the pitch at the edge and not
form the correct shape. It is also easier and quicker to make. Also a large
blob is first put in the centre of the tool and left to cool for a while
so as to provide depth to the centre to give shape during pressing. The rest
of the pitch is then added and allowed to flow evenly over the surface up
to and even over the edge. Do not worry about this as it can easily be chipped
off later when cool. The tool is left for only 30sec before splashing with
water and quickly placed and pressed into the mirror. If the lap has not
made full contact the put under hot running water, dispersing the flow, to
soften and then repeat the pressing.
after 2 sessions of 25mins each the centre of the mirror was seen to be getting
lower. After 2 hours the centre was getting well down but had low and raised
zones within it. Reworking with the larger lap when repressed would smooth
these out. Rochi lines where now straighter and less bent towards the
middle.
On Friday the 12 September Geoff and I did further work on the centre and
retested. The centre now had an 8" diameter hole but did not seem to be too
deep. We then decided to reform the main lap and evenout the work done by
the small lap. We heated the pitch that was left over from making the 8"lap
and cleaned the main lap. Pitch was painted on the low areas. After heating
the surface with a paint stripper and blowlamp we poured on hot water to
give a final overall heating of the lap. The lap was then well pressed in
and removed. The high spots where well grooved and the lap faceted all over.
It was then repressed two more times before use. We did an hours work doing
mainly backward and forward strokes and finishing with 10 minutes of W stroke.
The focult test and ronchi test showed a much-improved surface. The ronchi
lines where much straighter near the middle of the mirror and not curving
in. The focult test showed that the central hill had been planned down with
some of the central hole still remaining. Further work will be required to
gradually deepen the centre with care not to dig a too deep a hole therefore
using sparing bouts of the 8" tool together with the main lap to even out
any irregularities caused by the 8".
Work level was increased over the second week in October, as it was obvious
that the edge was going to take a long time to get done. Evening sessions
during the week and extra work on Sundays began to take effect on the edge.
Only the last 5mm had any significant pits on Sunday the 12th of October
after 6 hours polishing on Saturday and Sunday. I had my doubts that the
outer 5mm would ever polish due the pits in this zone being much larger than
the rest of the surface. This could be due to not carrying through fine grinding
enough on the edge. It may be best to stop work and figure and mask off this
very outer edge when aluminised. It would still be a 29 to 29.5 inch mirror,
which is still large!! The extra work required to remove these larger pits
would not be acceptable and be very costly in cerium oxide. (£100 to
date to polish the mirror!)
Building the testers for the
mirror
1)The focult tester
I had already completed a focult tester some weeks before to get some experience
in testing other mirrors. I had always held back from these optical tests
because the texts in books had always been obscure in the construction and
operation of the device. One book did give a more basic outline and I decided
to have a go. All you need is a 7watt-pigmy bulb, baton holder, piece of
flex and plug, short piece of drainpipe, few pieces of wood and a razor blade.
All items from B&Q (except the razor blade) for a few pounds. It took
only an hour to make it and I was testing my first mirror (my original 8.75
inch mirror) soon after. The mystery of optical testing soon began to subside.
The main objective left would be to understand how to take measurements of
these variations to get an accurate surface profile.
2) The ronchi tester
The Focult tester was adapted so that the ronchi tester could be used. This
was done using fine gauge transformer wire and two fine thread screws. The
screws where screwed sideways into a piece of wood that would be fixed to
the moving platform of the focult tester and positioned either side of the
same position that the knife edge would have been. Fine wire was then wrapped
around the threads and superglued into position. When dry one side of the
wire was cut away to leave a 48 lines per inch ronchi grating. This tool
was later to be used a lot during polishing to ascertain the general figure
of the mirror. The ronchi lines are very easy to see (more so inside focus)
and you get a feel for the overall shape of the mirror as the entire surface
is visible. The book Star Testing Astronomical Telescopes says that the ronchi
is no good at determining the fine figuring requirements of a mirror by looking
at the shape of the lines alone. The shape of the lines vary very little
between an undercorrected 1/2wave mirror and a perfect paraboloid. Actual
measurements must be taken to determine the true shape and
figure.
3) The Zonal Mask tester
This would turn out to be one of the main tests used to figure the mirror.
Only by measurement can the slope of the mirror be actually measured to say
if it is parabolic or not. Phil Layton, patron of the L.A.S., gave us the
first insight into how to use a zonal mask.
More details of the mask construction and use will be detailed here at a
later date.
Above image shows Dave Owen checking the edge of the mirror for pits. He is using a modified 25mm Orthoscopic eyepiece to determine how many are visible over a certain area.
Above iamge shows myself with one of the many graphs produced by the zonal mask measurements. This graph was one produced early in the figuring process.